Case Study about High Pressure Heater Utilization in a Local Power Generation Plant in Saudi Arabia
Journal: International Journal of Science and Research (IJSR) (Vol.8, No. 8)Publication Date: 2019-08-05
Authors : Abdulhamid Hussain; Mowffaq Oreijah; Mohammed Hassan; Muwaffaq Kensarh;
Page : 946-949
Keywords : Heat recovery; heat exchanger; power generation plant; fuel cost; unit efficiency; boiler efficiency;
Abstract
In this paper, there are two High Pressure Heaters (HPH) were out of service due to lake of maintenance. According to this issue, the unit efficiency decreased which consumed more fuel to compensate the temperature drop. During water circulating in a condensate water system there are heat waste, temperature drop, low performance and poor quantity of heat transfer which will cause an insufficient efficiency due to High Pressure Heaters (HPH) are not working properly. To remedy this issue, we study and focused on how efficiency can be improved when high pressure heaters in service and compare the results between the two situations in and out of service by calculate different parameters; TGHR, TNHR, Boiler efficiency and NUHR. Fuel cost effectiveness studied in this paper at maximum heat rate difference 11.8 kJ/ kWh.
Other Latest Articles
- Assessment of Groundwater Quality with Special Reference to Fluoride Concentration in Parts of Kandukuruvagu Basin in Nalgonda District, Telangana State, India
- Road Power Generation
- The Fauna of Insects of Vegetables and Melons of Central Fergana, Especially Its Distribution and Ecology
- MPPT for a PMSG Based Wind Turbine in a Grid Connected DC Micro Grid System
- The Effect of Profitability and Firm Size on Corporate Social Responsibility and Good Corporate Governance for Companies Listed on the Indonesia Stock Exchange
Last modified: 2021-06-28 18:22:28